On Saturday, July 10th at sunset, Key Westers gathered at the White Street Pier to protest the BP and its lack of corporate responsibility since the Deep Horizon blowout. Kelly Young and Erika Biddle led the event. Many citizens spoke out and signed a pledge to reduce their oil comsumption by 10%. Everyone hoped to send a message for a clean energy future.
Christian Science Monitor: Drilling moratorium: US cites weak spot in blowout preventers
http://www.csmonitor.com/USA/2010/0713/Drilling-moratorium-US-cites-weak-spot-in-blowout-preventers
The Obama administration on Monday cited control systems on subsea blowout preventers as one reason for its offshore drilling moratorium. But more than a year before the BP oil spill, authorities learned that balky control systems were the most common cause of blowout preventer failure.
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Oil and gas escape from the top of the new containment cap (black discharge at top-center) at the site of the Deepwater Horizon oil spill in the Gulf of Mexico, in this image captured from a BP live video feed July 13.
BP/Reuters
By Mark Clayton, Staff writer / July 13, 2010
Before he leaped into a lifeboat in the middle of the night on April 20, Christopher Pleasant tried to trigger a deep-sea safety device to squelch the oil-well blowout and fire raging aboard the Deepwater Horizon drill rig.
In those last frantic minutes in the rig’s central control room, Mr. Pleasant – a subsea superviser for Transocean, the rig’s owner – pressed two buttons simultaneously to activate a 450-ton blowout preventer sitting 5,300 feet below the sea surface. If its massive “shear ram” valve closed, it would slice through the drill pipe and stop the torrent of burning gas.
For one fleeting moment, the control panel lights offered a ray of hope – showing the shear ram and other BOP valves apparently closing. Valve indicator lights flicked from green (open) to red (closed), he told federal investigators in May in New Orleans.
Yet something wasn’t right. Another set of gauges just above the BOP control panel showed no hydraulic pressure at all – “no flow,” he testified. Also, the fire was still burning. So, despite BOP control system lights showing the shear-ram closed, it was not.
“I knew it was time to leave,” Pleasant testified.
No one knows yet just why the rig’s BOP did not work – or why the device’s hydraulic-electric control system gave Pleasant the wrong readings. That mystery won’t be solved unless the BOP is pulled off the sea floor months from now. But when the Obama administration on Monday issued a revised moratorium on drilling in the Gulf, it cited fresh concerns about the reliability of BOP control systems as one reason for its action.
Indeed, more than a year before Pleasant’s frantic efforts to stop an inferno, a large study of BOP reliability in the Gulf of Mexico had warned industry experts and federal safety officials that balky control systems were by far the most common cause of BOP failure – and apparently getting worse.
Altogether, 63 percent of blowout preventer test failures cited in that 2009 study, a joint effort by the industry and the regulatory US Minerals Management Service (MMS), involved control systems. By contrast, a similar study a decade earlier had found control systems were responsible for 51 percent of BOP failures.
Control systems are vulnerable to leaks
Blowout preventer control systems are hydraulic and electrical units housed in two waterproof pods – the electronic brains of the school-bus-size BOP stacks. The pods – one blue, one yellow – are identical systems, each a backup for the other. Hydraulic and electrical conduits run from the rig deck above the ocean’s surface to the pods on the sea floor.
But these control systems, many of them newer-generation units activated by microprocessors, are vulnerable to leaks and failures that can render a BOP useless, according to the closely held study, first reported by the Monitor.
Those microprocessor-based, or “multiplex,” control systems enable BOPs to respond in an instant to an electrical signal from the rig – a rate much faster in deep water than that of older, hydraulic-only systems. But there is a downside, too.
“These systems are newer within the industry and thus efforts to improve reliability have not been as extensive,” the 2009 study found. They “are much more complex, with more subsea components.”
Because the newer systems “have electrical and electronic components in the water; leaks are more likely to have significant consequences in these systems,” the report warned. After noting that hydraulic fluid may leak to the sea in some circumstances, the report states: “Leaks in electrical systems can be expected to render them inoperative.”
It was not the first such warning. A smaller 1999 study of BOP reliability in the Gulf had warned that “a single leakage can jeopardize complete BOP control.”
But the big new 2009 study, funded by the industry and the MMS, was focused on finding ways to cut the cost of BOP safety testing – with potential savings of about $193 million annually, the study’s prospectus estimated.
In fact, the study authors – West Engineering Services, a Texas consulting firm specializing in BOP technology – did recommend that the MMS relax its standards concerning how often to test several subsea BOP components. The study, for instance, recommended a reduced schedule for pressure testing of some BOP valves, from at least once every 14 days to once every 35 days. It recommended testing the shear ram valve just once in 77 days instead of once in 30 days. (See related story.)
Emphasis on testing control systems
But because control systems were found to be the part of the BOP most susceptible to failure, the report recommended no change to rules for testing control systems: at least once a week.
“It is important to understand and focus on the fact that control system failures are the most likely category of failures on subsea BOP equipment,” the authors wrote. “Even though control systems seem to have the larger margin of failures, due to redundancy there were not any cases where a control system failure would have compromised the well control abilities.”
While the control system failure rates may be accurate, the study’s conclusions are questionable, some industry veterans say.
Leaks of hydraulic fluid in deep water are the bane of BOP control systems and need more, not less, oversight, says Robert Bea, an engineer at the University of California at Berkeley who was a chief engineer for Shell Oil for 18 years and an expert reviewer for President Obama’s recent 30-day safety study on offshore drilling.
The BOP hydraulic lines of the Deepwater Horizon were leaking, according to the drill logs, he says.
“It’s like the brakes on your car. Those brakes get mushy when there’s a leak,” Dr. Bea says. “At some point they just won’t work. With a BOP, you don’t need much of a leak for that control system’s hydraulics to fail.”
The complexity of newer BOP control systems makes them vulnerable, says another BOP engineer who asked not to be named because he is still active in the industry. “The biggest problem with a BOP is the control system,” he says. “If a BOP has maybe 50 parts, then its control system has 500 parts. Many of them are vulnerable to water leaks.”
As part of the Deepwater Horizon’s last line of defense, a “dead man’s switch” in the BOP unit was supposed to trigger the shear ram, if both electrical and hydraulic communications with the rig were lost. But this system failed, too.
“We already know one of the battery pods [providing power to the BOP control system] was dead,” Bea says. “The other one was functional. But you have this system designed for redundancy, and because of neglected maintenance it is no longer redundant. It’s like going parachuting, but without a backup chute. We were relying on this BOP like a parachute – and when it came time, the backup didn’t work.”
‘The problem child’
The study shows that industry representatives reviewing the findings wrestled with their meaning and sought clarification about the vulnerability of control systems on BOPs. In an appendix to the 2009 study, unidentified industry officials commented on control system failures and asked the consultant about it.
“What’s being said [in the report] is that the control system is the problem child in the system, but redundancy is the savior?” the industry officials commented.
“Yes, control systems are the problem and redundancy is the savior,” the authors responded.
Officials at West Engineering did not return Monitor e-mails or phone calls. MMS officials, along with the Department of Interior, responded to e-mailed questions but refused requests for an interview.
Asked if the MMS had changed, or considered changing, its testing frequency for control systems, MMS said: “No, MMS has always required operators to function test annular and ram BOPs every 7 days between pressure tests.”
The MMS added that the 2009 study “is not an MMS study” and therefore the high frequency of control system failures was “proprietary” information that never became part of the agency’s safety research program data.
But key people at MMS did know of the control system problem. The agency provided funding for the study, several industry experts told the Monitor. Moreover, a prospectus for the study and the study itself both refer to a close partnership between BP, at least eight other oil companies, and the MMS.
Three senior MMS officials are listed in the study as involved and raising questions about it: Lars Herbst, regional director of the Gulf of Mexico OCS Region; William Hauser, chief of the Regulations and Standards Branch, and Kirk Malstrom, an agency petroleum engineer.
The Interior Department, which is coordinating media requests for the MMS during its reorganization, did not grant requests to interview those MMS officials. In review comments on the report, MMS officials asked questions about rig performance, failure detection, and a few other issues. None questioned the report’s central finding: the high rate of control system failures.
“This sort of touch-and-feel evolutionary approach to loosening testing standards is not good engineering,” says Bea, who has read the study. “I would never want to fly on an aircraft whose safety margins are regulated this way.”
Paul Helfer, a former senior engineer with BOP-maker Cameron International, who now does consulting work in the industry, says control system standards need reexamination and a new set of testing requirements.
“It’s a pretty good chore to ensure a control system works and stays working,” he says. “That has to include some serious testing.”
Special thanks to Richard Charter
Wall Street Journal: Spill Panel to Press Obama Team on Drilling Ban
BUSINESS
JULY 14, 2010
By STEPHEN POWER
NEW ORLEANS-The leaders of a presidential panel investigating the Gulf of Mexico oil spill expressed skepticism Tuesday about a six-month moratorium on deepwater oil drilling and said they would press the Obama administration on why a prolonged ban is needed.
“We’re going to look over their shoulder and have some comments to make as to whether we think the judgments they made are appropriate,” said Bob Graham, one of the two co-chairmen of the National Commission on the BP-Deepwater Horizon Oil Spill and Offshore Drilling.
The comments by Mr. Graham and William K. Reilly represent a sharp shift. A day earlier, both men had said that assessing the merits of the moratorium wasn’t part of their panel’s mission.
But on Tuesday, during a break in the second of two days of hearings on the environmental and economic impact of the spill, Messrs. Reilly and Graham said they had been persuaded by Louisiana elected officials, business people and ordinary citizens to weigh in on the issue.
Mr. Reilly said he was “quite moved” by the testimony of Sen. Mary Landrieu (D., La.), who said the government should be able to move faster than six months to determine the safety levels of the 33 rigs covered by the ban. Mr. Reilly said he was also surprised that representatives of Louisiana’s fishing industry, which has been rocked by the spill, had called for lifting the moratorium.
“Frankly, I have less understanding why it’s going to take so long to reassure people that the existing rigs are safe,” Mr. Reilly said during a news conference with Mr. Graham. Mr. Graham drew an analogy to a recent order by the Federal Aviation Administration directing airlines to inspect the cockpit window heaters on roughly 1,200 Boeing airliners, amid concerns that the heaters could have contributed to incidents involving in-flight fires, smoke and shattered windshields.
“I’m sure they [aviation companies] didn’t wait until all 1,200 airplanes had been evaluated to release the first ones” back into service, Mr. Graham said. “Why couldn’t we have something like that with these [drilling] rigs, once we’re satisfied they have met safety guidelines and the [Interior] Department is satisfied with its capacity to” carry out and enforce relevant safety rules.
Messrs. Graham and Reilly spoke after hearing testimony from the director of the Bureau of Ocean Energy Management, Regulation and Enforcement, Michael Bromwich. Mr. Bromwich said the administration continues to believe a temporary ban on deepwater drilling is necessary, not only to give the government sufficient time to implement new safety measures but also to investigate the cause of the April 20 explosion of the Deepwater Horizon rig.
Mr. Bromwich said the oil and gas industry needs to “show us and show the public they have developed more effective containment strategies” for dealing with oil spills “than they have developed to date.” The administration has said its moratorium on deepwater drilling will continue until Nov. 30 or “such earlier time that” Interior Secretary Ken Salazar determines that such operations can proceed safely.
The Interior Department on Monday issued an order banning most new deepwater-drilling activities until Nov. 30. The ban replaces an order issued by the department in May that was struck down by a federal court last month, and sets up the possibility of a fresh legal challenge. Hornbeck Offshore Services, which challenged the initial moratorium, declined to comment.
It’s not clear how the Interior Department’s new moratorium will affect litigation between the oil industry and the Obama administration over the earlier ban. A Justice Department spokeswoman said that Mr. Salazar’s new order “expressly supersedes” the earlier one. As a result, she said, the administration plans to ask the U.S. District Court for the Eastern District of Louisiana to dismiss a lawsuit filed by the oil industry against the government over the earlier ban.
But Carl Tobias, a law professor at the University of Richmond in Virginia, said he thought it unlikely that the judge in the case, Martin Feldman, would grant the administration’s request. “It’s a new order, but he still has jurisdiction over the subject matter,” Mr. Tobias said. “I think he’d try to maintain that.”
Messrs. Graham and Reilly didn’t commit to issuing a formal conclusion on the moratorium by a specific date. Mr. Reilly said the speed with which the commission could move to examine the issue would be determined by how quickly it can hire additional staffers. The Obama administration is seeking $15 million to fund the panel, but Congress has yet to approve the request, forcing the panel to rely on temporary funding from the Energy Department.
Nevertheless, Mr. Reilly said, “we probably have a contribution to make to the thinking” on the moratorium.
Mr. Reilly said he also wants the panel to quickly address the use of chemical dispersants in combating the spill, and whether they have affected the environment even more than the spill.
“The major question for this commission, and one we haven’t fully resolved, is whether this [accident] was a one-off event or [evidence of] a systemic weakness in the technology of deep-sea drilling,” Mr. Reilly said.
Write to Stephen Power at stephen.power@wsj.com
Special thanks to Richard Charter
Coral-list: Oil Spills Bibliography – developed & offered by the NOAA Library
In support of research on oil spills, response, and restoration, the
NOAA Central Library published the /Oil Spills Bibliography/.
Below please find some general information about this product:
Librarians, Anna Fiolek, Linda Pikula, and Brian Voss, in collaboration
with the Library Staff, developed a document entitled: /Resources on Oil
Spills, Response, and Restoration: a Selected Bibliography/. This
document, also called /Oil Spills Bibliography/, has been prepared as an
aid for those seeking information concerning the Deepwater Horizon oil
spill disaster in the Gulf of Mexico and information on previous spills
and associated remedial actions. Various media products (web, video,
printed and online documents) have been selected from resources
available via the online NOAA Library and Information Network Catalog
(NOAALINC). Many of the resources included have been produced by NOAA
offices and programs. The content of the Bibliography includes
information sources concerned both with the harmful effects of oil and
chemical spills to marine habitats and their associated living marine
resources and with the cultural and economic impacts caused by such spills.
The /Bibliography/ is published online as Library and Information
Services Division current references 2010-2 at:
http://docs.lib.noaa.gov/noaa_documents/NESDIS/NODC/LISD/Central_Library/current_references/current_references_2010_2.pdf
(PDF version)
http://docs.lib.noaa.gov/noaa_documents/NESDIS/NODC/LISD/Central_Library/current_references/current_references_2010_2.docx
(Microsoft Word version).
We hope the Coral-List Community will find this product useful.
Cheers, Anna.
—
Anna Fiolek, Metadata Librarian
NOAA Central Library
1315 East-West Highway
SSMC3, 2nd Floor
Silver Spring, MD 20910
Tel. 301-713-2607, ext. 147
Fax: 301-713-4599
E-mail: Anna.fiolek@noaa.gov
Library home page: http://www.lib.noaa.gov
/The opinions expressed in this email do not necessarily
reflect the views of the U.S. Government/
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Art from the Spill
This song is written and performed by Katherine Archer, who lives in St. Augustine.
















